Pitot system - odd event
On tow the other day the airspeed indicator jammed and the digital airspeed read about 20kts too high. When I got down the digital airspeed was 30kts with the glider stopped, and turning off the unit (S80) and re-initialing the tas read 30kts. Upon examination the diaphragm was found to be ruptured in the winter, and auto zeroing the pressure sensors on the S80 left the tas navbox with no reading (---) indicating the transducer was likely damaged.
Something clearly sent a shock through the pitot system, perhaps a bug hit square in the inlet.
Air moves through the pitot tube when blowing into the tube from the panel end.
If any of you have experienced something like this before, I would appreciate your insight on this issue. I am reluctant to attach a new instrument to the system until I've taken basic precautions testing the system. Could there be a partial blockage that might shift and shock the system again? What procedures are there to establish the integrity of the pneumatics?
Many thanks for any ideas on this.
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