A aviation & planes forum. AviationBanter

If this is your first visit, be sure to check out the FAQ by clicking the link above. You may have to register before you can post: click the register link above to proceed. To start viewing messages, select the forum that you want to visit from the selection below.

Go Back   Home » AviationBanter forum » rec.aviation newsgroups » Home Built
Site Map Home Register Authors List Search Today's Posts Mark Forums Read Web Partners

what went wrong



 
 
Thread Tools Display Modes
Prev Previous Post   Next Post Next
  #1  
Old August 7th 07, 11:07 PM posted to rec.aviation.homebuilt
Dick[_1_]
external usenet poster
 
Posts: 71
Default what went wrong

Having spent 4-1/2 hours removing and 1 hour replacing a leaking split seal
on the front of my flanged crankshaft C-85 , my first flight today still
shows leakage....

Never really doing those old Chevy two part split seals well, I guess I'm
still inept G.

I think I'll be able to better the aforementioned time durations but would
appreciate any hints at doing a better job this time.

Thanks, Dick


 




Thread Tools
Display Modes

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

vB code is On
Smilies are On
[IMG] code is On
HTML code is Off
Forum Jump

Similar Threads
Thread Thread Starter Forum Replies Last Post
what am I doing wrong gt[_2_] Aviation Photos 8 June 4th 07 01:49 AM
Wrong Vario!!! Mike Hostage Soaring 0 March 30th 05 01:39 AM
What's wrong with this engine? Fred the Red Shirt Home Built 6 May 3rd 04 04:49 AM
ATC says wrong position Greg Esres Instrument Flight Rules 28 April 30th 04 05:37 PM
Saying the wrong thing...! Paul Sengupta Piloting 3 January 23rd 04 03:58 AM


All times are GMT +1. The time now is 03:35 PM.


Powered by vBulletin® Version 3.6.4
Copyright ©2000 - 2025, Jelsoft Enterprises Ltd.
Copyright ©2004-2025 AviationBanter.
The comments are property of their posters.